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Research of wet string grid dust removal vehicle and creation of dust control area on tunnel working face.
Deng, Huan; Chen, Shiqiang; Huang, Junxin; Wu, Zhirong; Rao, Ying; Qiu, Xinyi; Cheng, Jiujun.
Afiliação
  • Deng H; School of Civil Engineering, Hunan University of Science and Technology, Xiangtan, 411201, Hunan, China.
  • Chen S; School of Civil Engineering, Hunan University of Science and Technology, Xiangtan, 411201, Hunan, China. shiqiangchen@hnust.edu.cn.
  • Huang J; School of Chemical and Environmental Engineering, Hunan Institute of Technology, Hengyang, 421000, China.
  • Wu Z; School of Energy and Built Environment, Guilin Institute of Aerospace Technology, Guilin, 541000, Guangxi, China.
  • Rao Y; School of Civil Engineering, Hunan University of Science and Technology, Xiangtan, 411201, Hunan, China.
  • Qiu X; School of Civil Engineering, Hunan University of Science and Technology, Xiangtan, 411201, Hunan, China.
  • Cheng J; School of Civil Engineering, Hunan University of Science and Technology, Xiangtan, 411201, Hunan, China.
Sci Rep ; 14(1): 8292, 2024 Apr 09.
Article em En | MEDLINE | ID: mdl-38594304
ABSTRACT
The spread of blast dust throughout the tunnel becomes a common problem in drill and blast tunneling,the key to breaking through the problem is the creation of a dust control area on the working face.In view of this key problem, a wet string grid dust removal crawler vehicle was developed, the power of the vehicle came from the diesel generator, and further, the air cooler of the diesel generator was used to generate airflow, and the suction process formed by the on-board axial flow fan was coupled to create a dust control area of the working face after blasting.The results show that when the frequency of the axial flow fan is adjusted to 30 Hz, the airflow speed of the wet chord grid section reaches 3.34 m/s, and the dust removal efficiency is the highest, with a value of 94.3%.Compared with the non-use of the dust removal vehicle, when the air outlet of the air cooler is front, horizontal front, horizontal rear, the dust concentration is reduced by 74.37, 92.39 and 50.53%.Finally, the optimized wet grid dust removal crawler was installed in the Dading tunnel, and the actual dust reduction efficiency was about 78.49%. The results obtained provide an important technical way to improve the working environment of the drilling and blasting construction tunnel.
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Texto completo: 1 Base de dados: MEDLINE Idioma: En Ano de publicação: 2024 Tipo de documento: Article

Texto completo: 1 Base de dados: MEDLINE Idioma: En Ano de publicação: 2024 Tipo de documento: Article